sorry to anger you escort lover.
I blew up the motor cause I was mad and I wasnt going to use it anyway. the motor still had alot of work that needed to be done and it was taking up space. yeah, I could have parted it out but what the fun be in that? I mean damn, we have shows dedicated to watching stuff break so I think my only fault was not going and getting a video camera for the event.
I forget who said what but yeah I m sure 16 psi was doing nothing but leaning it out. The T3 was too damn huge and the GST wastegate was not right. Like I said, it needed more work that was never gonna get done. It drove pretty good around town but my WOT run was the death of it.
or it could have been the nitrous.
My intention was to pop it but after it didnt break in 15 miles, I thought I might have just installed a motor that would survive. I started to think that maybe I just crossed the barrier and I should go home and tweak the fuel so it would last. Then certain circumstances and a bi-polar problem caused me to put it through its paces. It was an impressive failure. First motor Ive ever blown and I'll never forget the sound as long as I live. Kinda like being in your first crash. Its almost a sickening noise. well it would be if you cared about your engine. I think a that junkyard powertrain went out in the most admirable way possible. I salute you noble SPI motor and blown T3.
Sorry I haqvent been back to update till now. I ran into problems reinstalling the old beast and it took me like 20 hours to get it all back together. I havent even slept yet.
Finally got it rebuilt and tested. All is operating normally and the car is good again. Im just glad I didnt have enough time to get used to the turbo, otherwise Id probablly be disappointed with it.